Matt Yorke
Building the Exhaust
Time to build the exhaust system – a bit of a challenge to make sure it clears both the chassis and bodywork.

Alternator Mount
I tried quite hard to mount the alternator on the OS of the car, modifying the original mount. But I’ve actually mounted the engine so low in the chassis that the alternator fouled – so I had to come up with a neat custom solution:

Driveshafts
The CV Joints arrived so I spent a bit of time mocking up the first driveshaft with some 25mm tube.
(more…)Gear Linkage
With a far too long hiatus, I spent some time over christmas 2023 doing the gear linkage. It’s just mocked up for now (hence jubilee clips and over-length rods), but works really well and all gears fit in the perfectly.

New Throttle Body for the Ultima
Time to crack on a bit more. In the interim, I’ve made new cooling pipes that run front to rear, which included getting my head stuck in the side pod of the car and having a bit of a panic when I couldn’t get it back out. But that’s not interesting.
The challenge was can I avoid turning a 3kg chunk of billet aluminium into scrap and instead turn it into 500g of something useful.
The idea is twofold. To switch the throttle body on my V8 from the back of the inlet manifold to the front, AND to ditch the large, heavy and complex mechanical throttle body and replace it with a really slick & elegant DBW throttle body.

From clerk to Spitfire pilot
Reproduced from “The News”, Saturday September26th, 1992
After surviving the bombing of his home and his Portsmouth workplace, Ray Wells was one of only two pilots in his wartime Spitfire squadron who came through alive. Now secretary of Langstone Sailing Club, he talked to Robert Lindsay about his war years
I was a British Rail clerk at the Fratton Road depo and was standing out on Goldsmith Avenue when it happened. It was just a lone raider on a day-time raid.
We saw this plane but there was no air raid warning or anything so we all wondered what was happening. We were looking up at it and we saw something detach from the fuselage and we thought “What the hell is that?”. Then we realised what is was and went flat on the ground.

It fell on the end of the freight depot and damaged it quite severely, one or two people were injured but no one was killed.
I used to live in Lichfield Road at Copnor which was heavily blitzed. Each cluster of bombs made a kind of whistling screech as they fell through the air. I can remember being in the shelter there counting the number of salvoes you could hear. I got up to 80-odd! The landmines didn’t make a noise because they came down on parachutes.
Our house was damaged and Cuthbert Church was ruined and had to be totally rebuilt.
By the time I was 18 in September, 1941, I had eventually managed to get into the Air Force. At that time, after the Battle of Britainm everyone wanted to join. Though I was only a lowly clerk I thought I would have a go and got through.
I never thought I would attain the heights of a pilot, but I found I was just as good as the university graduates and the doctors and dentists I was with.
After training in America and Britain, I was finally posted to 19 Spitfire Squadron in August 1943.

I was with 19 Squadron all the way through D-Day and the war through Belgium and Brussels. I flew 115 operations. I was a bit over the top because you were only supposed to fly about 20 ops on a tour then you were meant to be give a rest.
There was myself and one other chap. We were the only two left out of a force of 90-odd pilots, The rest were either killed, prisoners of war or just didn’t make it through for other reasons.
The worst bit was the waiting around to fly. The actual flying was all right. It was the bit between that got a bit strained. You were losing people all the time and were wondering if you were going to be next.
I had a few dog-fights all right. I shot down four German fighters, Focke Wulf 190s. I was damaged twice, both times by flak, once over Le Havre when it was enemy hands and once right over Germany, but I managed to get back all right.
On a rest
Just towards the end of the war, to give me a rest, they post me to the RAF Film Production Unit at Pinewood Studios. We took cameramen up over Germany so that they could take stills and newsreel film of the bombing.
I even had to take them to film out men crossing the Rhine. I had to fly under out own artillery fire at about 200ft and then turn to follow the river, tilting the aircraft so that the cameraman could take his shots out of the window! I was supposed to be on a rest!
After the war I want back to British Rail as a clerk again and I worked my way up so that by the time I retired I was a project officer on computers.
I was given the opportunity to carry on flying, but it just wasn’t my cup of tea. They needed people from universities. I’d just been to Portsmouth Polytechnic where I’d trained to be a pattern-maker in the dockyard. I didn’t have the right background.
Audi C5 RS6
Man Maths
Just before the twins were born in 2015, I decided that we needed a spare family car – we had an one, but it would be useful to have 2 cars capable having kids in the back. A bit of googling told me that the standard Audi A6 isofix bars bolted straight in to the back of the RS6. And I am a bit of a petrolhead – and the cars were cheap! A Plan started to come together…..
Lots of looking at the RS6s for sale at the time – many clearly in very poor condition, with some being crazy money. Eventually I came across this one:

What stood out about this one was that it seemed relatively decent and untouched, but even better, was black but didn’t have the white leather interior. I don’t like white leather – instead, this one had the black alcantara with aluminium trim interior, which is a rarer combo and I think it really works! So a few thousand £ later and the learning journey started. I’d read all about the weaknesses of these cars and that all the solutions are – but I figured it wouldn’t need ALL of them doing – would it?
Engine Out – Part 1
Eventually I found the torque converter wasn’t locking up correctly, despite the gearchanges still being silky smooth. I did a gearbox service with new oil and filters – the oil came out looking manky. The TC valiantly tried to lock up, but just couldn’t manage it.
Audi claim these gearboxes are sealed for life, but ZF themselves make a service kit for them and it’s well known that an occasional gearbox oil change is required to make the gearboxes last – what Audi really mean is they’re sealed until the warranty expires. So I bit the bullet and removed the engine to do the torque converter and gearbox – for the first time. I’ve built or rebuilt loads of things before – but never in what I’d call “modern generation” cars. What I mean is in a car where everything is designed by CAD and crammed in, but gives no acknowledgement of needing to service things! It is a complex and tight fit in there. But we got there in the end and while it’s a lot of work, it’s actually not hard as long as you’re patient and methodical

That job all went OK – you can see the new gearbox in the pic above – and bolted it all back together. The car ran well – but now it was loosing a little coolant! This was the moment where I learnt that the list of things to look for on a C5 RS6 are not “maybe” things – they will happen, it’s just a question of when. The little plastic pipe that connects the oil cooler to the engine block had fractured – the notorious “bufkin” pipe. So it was time to pull the engine again! Argh!
Engine Out – Part 2
This time, I decided “lesson learnt” and went in to it much more fully, including not just replacing the bufkin pipe with the lovely alloy machined one you can get, but replacement intercoolers (Audi ones always leak, even when new), shortening one of the hard cooling pipes that prevents you from removing the RHS rocker cover unless you remove the engine (what moron designed that!)

Replaced the DRC entire DRC setup (another when, not “if” thing that fails) with Koni shocks – and had all the steel suspension arms and springs powdercoated too:


At the same time, also had the turbos rebuilt with new cartridges by Owen Developments. Stock – other than upgrading the thrust bearings in the turbos to 360 degree ones for better longevity. Also used the opportunity to replace the plastic shoes on the cam adjusters – they are known to wear at about the 80K mark and if they disintegrate, it causes a right mess.
I’ve sort of lost track of everything I did to it – it’s all noted down in a spreadsheet somewhere – but I also tidied up the engine bay and replaced the inlet hoses (that always collapse) with some nice silicone ones. I think it looks smart – I’ve actually replaced the black inlet ducts with carbon ones that match the air filter covers now – they are lovely.

Brakes
At some point, I decided to redo all the brakes. New rear calipers are easy to source, but the fronts are a bit more special – so I had them rebuilt. With hindsight, I think I could have saved myself a chunk of money by doing it myself, but the convenience of having someone else do it was appreciated:


I think the calipers came out OK, although I think I overpaid:

You can see I both powdercoated the backplates at the same time, and also replaced the lower wishbones with new:

That Plastic Bit
There’s a really nasty plastic air duct at the front of the cars, that channels air through the oil coolers. It’s simultaneously floppy and yet also brittle – and annoyed me every time I went near it. So I decided to make a new one out of some nice NS4. The hateful plastic bit:

Starting to make a new kit of ali parts:

Assembled on the workbench with the old bit behind:

And on the car. I think it came out OK:

Today
That’re pretty much where it is today. All the stuff that they need doing – is now done, and I can by and large enjoy the car. Currently waiting on some new wing mirror glass to arrive and is due a bit of a service – but the effort above was all worth it and the car all just works now.
Ultima Spyder Rebuild
I built this Spyder back in 1997 with a Renault 25 V6 Turbo motor & UN1 Gearbox.
It was good and I was a fairly early adopter of building a kit car with an EFI motor, especially turboed.

It always ran well – but time passes and I decided a few years back to re-engine it.
I bought an engine, gearbox, custom flywheel & clutch for it – and then parked it for another few years…
Bravo Drive Rebuild
I found my Bravo drive was making an unhealthy sound when running the motor on the hose:
That’s not right. Removing the top cap and having a look at the bearings, it all becomes clear:

Infortunately, the water damage also included the bearings in the gears:

So there was nothing for it other than a full strip down and rebuild. This is the pinion gear – every bearing showed some damage, and the big bearings are only available as part of a full kit of gears:

A fairly expensive round of ordering and the rebuild could start:


Carefully put it all back together using all the necessary special tools:

Major bits back in:

Checking pinion gear backlash:

And finally pressure testing it all:
