Background
The engine started life as a Mercruiser Bulldog 540, originally part of a triple engine setup on a sunseeker.
Apparently the sunseeker ended up sinking when the engines were virtually new and they were removed and written off by the insurance. The engine then sat in my friend, Tony Davis’ garage for a few years.

When I got the engine, I knew I wanted to improve it a bit to take full advantage of the bulldog “tall deck” block and increased capacity, but without going supercharged or turbo. I always loved the “stack” intake manifolds you see on retro & vintage racing cars and I liked what kinsler had done on some of the mercruiser engines, so I thought this might be an interesting path. I found a small bore hillbore manifold that looked like I could convert it to EFI, along with a set of Eickert exhaust manifolds and mocked it all up:

This looked like it would all fit together, so I worked with Bob Madara (rmbuilder on OSO) to put a spec together. This is the specification we ended up with. It meant I would need to run exhaust dry to the tips, but should also give a nice idle, strong torque all the way up, with peak horsepower at about 5500rpm.
Specifications
| Bore | 4.5″ |
| Stroke | 4.375″ |
| Capacity | 556.7 cu (9.1 litres) |
| Compression Ratio | 9.56 |
| Exhausts | Keith Eickert Cast Headers |
| Cyinder Heads | Airflow Research 315cc with Inconel Valves & Anodising |
| Intake Manifold | Hilborn 2 7/16 Mechanical Injection |
| Fuel & Ignition | Megasquirt 2 V3 running Bank Fired injectors and Wasted Spark ignition |
| Camshaft | Custom Marine Kinetics Grind (see below) |
| Crankshaft | Lunati Signature Series |
The camshaft was designed by Bob Madara with the following specs:

Modelling this all in desktop dyno, it looks good. I know the numbers aren’t doing to be “real world” accurate, DD is inevitably a bit enthusiatic on the numbers and is crank, not propshaft, hp. But anyway, this should produce an engine with similar power to the mercruiser 600 supercharged motors and should “just” be OK on a Bravo XR drive. The engine will never be dynoed to verify, but it’s nevertheless good to see some nice high volumetric efficiency numbers (we have all the head flow numbers entered correctly) on a big block chevrolet motor.


This set the recipe, so a few wise purchases later, along with having the block bored out slightly and a crank journal machined, I was ready to start assembling it all.
The Build
The block was bored from 4.44 to 4.5″ bore, leaving enough meat still in it for a rebore in future if needed (that would then make it a 572 as well). After cleaning all the block very carefully, new cam shells were pressed in to the block:

And the bottom end assembled:

so far so good

Next the cam was installed and timed:

And the heads, along with the scorpion marine duty roller rockers:

Including using test springs to work out that stock length pushrods were OK:

And the intake manifold:

It started to look decent:

And eventually it all came together pretty well:

Lessons
I learnt quite a few things duiring the build, here’s 3:
Avoid the single piece steel core sump gaskets – of it you do use them, use them carefully. I had a leak where one was a bit too thick and didn’t compress down properly – which meant engine out of the boat again tp put a traditional 4-piece sump gasket in.
The 140 amp single V-pulley alternators from DB Electrical are excellent value for money
Always use the bypass hose on the circulating coolant pump. I originally rigged my engine without this, making the block “full flow” – which also works for the full flow heat exchanger I have. Bad move. Without the little bypass hose on the reciculating pump, it generates enough back pressure to blow the core plugs of the engine. I wouldn’t have believed it if I hadn’t seen it. One popped out at fast idle on the hose – I assumed I had not put it in properly. One then popped out when I was out on the water – so I pulled the engine out to investigate properly and found that a 3rd would have come out, except it had wedged itself against the engine mount. Since re-installing the bypass hose, all is fine again.



































































